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LTC3717 Datasheet, PDF (13/20 Pages) Linear Technology – Wide Operating Range, No RSENSE Step-Down Controller for DDR/QDR Memory Termination
LTC3717
APPLICATIO S I FOR ATIO
When the voltage on RUN/SS reaches 1.5V, the LTC3717
begins operating with a clamp on ITH of approximately
0.9V. As the RUN/SS voltage rises to 3V, the clamp on ITH
is raised until its full 2.4V range is available. This takes an
additional 1.3s/µF. The pin can be driven from logic as
shown in Figure 5. Diode D1 reduces the start delay while
allowing CSS to charge up slowly for the soft-start func-
tion.
After the controller has been started and given adequate
time to charge up the output capacitor, CSS is used as a
short-circuit timer. After the RUN/SS pin charges above
4V, if the output voltage falls below 75% of its regulated
value, then a short-circuit fault is assumed. A 1.8µA cur-
rent then begins discharging CSS. If the fault condition
persists until the RUN/SS pin drops to 3.5V, then the con-
troller turns off both power MOSFETs, shutting down the
converter permanently. The RUN/SS pin must be actively
pulled down to ground in order to restart operation.
The overcurrent protection timer requires that the soft-
start timing capacitor CSS be made large enough to guar-
antee that the output is in regulation by the time CSS has
reached the 4V threshold. In general, this will depend upon
the size of the output capacitance, output voltage and load
current characteristic. A minimum soft-start capacitor can
be estimated from:
CSS > COUT VOUT RSENSE (10 – 4 [F/V s])
Generally 0.1µF is more than sufficient.
Overcurrent latchoff operation is not always needed or
desired. The feature can be overridden by adding a pull-
up current greater than 5µA to the RUN/SS pin. The
additional current prevents the discharge of CSS during a
fault and also shortens the soft-start period. Using a
resistor to VIN as shown in Figure 5a is simple, but slightly
increases shutdown current. Connecting a resistor to
INTVCC as shown in Figure 5b eliminates the additional
shutdown current, but requires a diode to isolate CSS . Any
pull-up network must be able to pull RUN/SS above the
4.5V maximum threshold that arms the latchoff circuit
and overcome the 4µA maximum discharge current.
INTVCC
VIN
3.3V OR 5V
RUN/SS
D1
RSS*
CSS
(5a)
RSS*
D2* RUN/SS
2N7002
CSS
3717 F06
*OPTIONAL TO OVERRIDE
OVERCURRENT LATCHOFF
(5b)
Figure 5. RUN/SS Pin Interfacing with Latchoff Defeated
Efficiency Considerations
The percent efficiency of a switching regulator is equal to
the output power divided by the input power times 100%.
It is often useful to analyze individual losses to determine
what is limiting the efficiency and which change would
produce the most improvement. Although all dissipative
elements in the circuit produce losses, four main sources
account for most of the losses in LTC3717 circuits:
1. DC I2R losses. These arise from the resistances of the
MOSFETs, inductor and PC board traces and cause the
efficiency to drop at high output currents. In continuous
mode the average output current flows through L, but is
chopped between the top and bottom MOSFETs. If the two
MOSFETs have approximately the same RDS(ON), then the
resistance of one MOSFET can simply be summed with the
resistances of L and the board traces to obtain the DC I2R
loss. For example, if RDS(ON) = 0.01Ω and RL = 0.005Ω, the
loss will range from 15mW to 1.5W as the output current
varies from 1A to 10A.
2. Transition loss. This loss arises from the brief amount
of time the top MOSFET spends in the saturated region
during switch node transitions. It depends upon the input
voltage, load current, driver strength and MOSFET capaci-
tance, among other factors. The loss is significant at input
voltages above 20V and can be estimated from:
Transition Loss ≅ (1.7A–1) VIN2 IOUT CRSS f
3. INTVCC current. This is the sum of the MOSFET driver
and control currents. This loss can be reduced by supply-
ing INTVCC current through the EXTVCC pin from a high
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