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9602 Datasheet, PDF (4/8 Pages) National Semiconductor (TI) – Dual Retriggerable, Resettable One Shots
Operating Rules (Continued)
B Use with high inverse leakage current electrolytic ca-
pacitors
The diode in this configuration prevents high inverse
leakage currents through the capacitor by preventing
an inverse voltage across the capacitor The use of
this configuration is not recommended with retriggera-
ble operation
t 0 3 RCX
TL F 6611–5
C Use to obtain extended pulse widths
This configuration can be used to obtain extended
pulse widths because of the larger timing resistor al-
lowed by beta multiplication Electrolytics with high in-
verse leakage currents can be used
R k RX (0 7) (hFE Q1) or k 2 5 MX whichever is the
lesser
RX (min) k RY k RX (max)
(5 kX s RY s 10 kX is recommended)
Q1 NPN silicon transistor with hFE requirements of
above equations such as 2N5961 or 2N5962
t 0 3 RCX
7 Input Trigger Pulse Rules (See Triggering Truth Table)
TL F 6611 – 8
Input to Pin 5(11)
(Pin 3(13) e HIGH)
Pin 4(12) e LOW
t1 t3 e Min Positive Input Pulse Width l 40 ns
t2 t4 e Min Negative Input Pulse Width l 40 ns
TL F 6611 – 9
Input to Pin 4(12)
(Pin 3(13) e HIGH)
Pin 5(11) e HIGH
8 The retriggerable pulse width is calculated as shown be-
low
 J1
tW e t a tPLH e K RX CX
1a
RX
a tPLH
TL F 6611–6
This configuration is not recommended with retriggera-
ble operation
5 To obtain variable pulse width by remote trimming the
following circuit is recommended
TL F 6611 – 10
The retrigger pulse width is equal to the pulse width (t) plus a delay time For
pulse widths greater than 500 ns tW can be approximated as t Retriggering will
not occur if the retrigger pulse comes within 0 3 CX (ns) after the initial trigger
pulse (i e during the discharge cycle)
9 Reset Operation An overriding clear (active LOW level)
is provided on each one shot By applying a LOW to the
reset any timing cycle can be terminated or any new cy-
cle inhibited until the LOW reset input is removed Trigger
inputs will not produce spikes in the output when the re-
set is held LOW
TL F 6611–7
6 Under any operating condition CX and RX (min) must be
kept as close to the circuit as possible to minimize stray
capacitance and reduce noise pickup
TL F 6611 – 11
10 VCC and Ground wiring should conform to good high
frequency standards so that switching transients on VCC
and Ground leads do not cause interaction between one
shots Use of a 0 01 to 0 1 mF bypass capacitor be-
tween VCC and Ground located near the DM9602 is rec-
ommended
For further detailed device characteristics and output performance please
refer to the NSC one-shot application note AN-366
4