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MIC4575 Datasheet, PDF (5/12 Pages) Micrel Semiconductor – 200kHz Simple 1A Buck Voltage Regulator
MIC4575
Functional Description
The MIC4575 is a variable duty cycle switch-mode regulator
with an internal power switch. Refer to the block diagrams.
Supply Voltage
The MIC4575 operates from a +4V to +24V unregulated
input. Highest efficiency operation is from a supply voltage
around +15V.
Enable/Shutdown
The shutdown (SHDN) input is TTL compatible. Ground the
input if unused. A logic-low enables the regulator. A logic-
high shuts down the internal regulator which reduces the
current to typically 50µA.
Feedback
Fixed versions of the regulator have an internal resistive
divider from the feedback (FB) pin. Connect FB directly to the
output line.
Adjustable versions require an external resistive voltage
divider from the output voltage to ground, connected from the
1.23V tap to FB.
Duty Cycle Control
A fixed-gain error amplifier compares the feedback signal
with a 1.23V bandgap voltage reference. The resulting error
amplifier output voltage is compared to a 200kHz sawtooth
waveform to produce a voltage controlled variable duty cycle
output.
Micrel
A higher feedback voltage increases the error amplifier
output voltage. A higher error amplifier voltage (comparator
inverting input) causes the comparator to detect only the
peaks of the sawtooth, reducing the duty cycle of the com-
parator output. A lower feedback voltage increases the duty
cycle.
Output Switching
When the internal switch is on, an increasing current flows
from the supply VIN, through external storage inductor L1, to
output capacitor COUT and the load. Energy is stored in the
inductor as the current increases with time.
When the internal switch is turned off, the collapse of the
magnetic field in L1 forces current to flow through fast
recovery diode D1, charging COUT.
Output Capacitor
External output capacitor COUT provides stabilization and
reduces ripple.
Return Paths
During the on portion of the cycle, the output capacitor and
load currents return to the supply ground. During the off
portion of the cycle, current is being supplied to the output
capacitor and load by storage inductor L1, which means that
D1 is part of the high-current return path.
Applications Information
The applications circuits that follow have been constructed
and tested. Refer to Application Note 15 for additional
information, including efficiency graphs and manufacturer’s
addresses and telephone numbers for most circuits.
For a mathematical approach to component selection and
circuit design, refer to Application Note 14.
6V to 24V
C1
150µF
35V
5 SHDN
SW 2
MIC4575-3.3BT
1 VIN
FB 4
GND
3
L1
68µH
D1
1N5819
3.3V/1A
C2
330µF
16V
8V to 24V
C1
150µF
35V
5 SHDN
SW 2
MIC4575-5.0BT
1 VIN
FB 4
GND
3
L1
68µH
D1
1N5819
5.0V/1A
C2
330µF
16V
C1 Nichicon
C2 Nichicon
D1 Motorola
L1 Sumida
L1 Bi
UPL1V151MPH, ESR = 0.12Ω
UPL1C331MPH, ESR = 0.12Ω
1N5819
RCH106-680K, DCR = 0.22Ω
HM77-11003, DCR = 0.233Ω, Note 2
Figure 1. 6V–24V to 3.3V/1A Buck Converter
Through Hole
16V to 24V
C1
68µF
63V
5
SHDN
2
SW
MIC4575BT
1 VIN
4
FB
GND
3
C1 Nichicon
C2 Nichicon
D1 Motorola
L1 Sumida
L2 Bi
UPL1J151MPH, ESR = 0.12Ω
UPL1C331MPH, ESR = 0.12Ω
1N5819
RCH106-680K, DCR = 0.22Ω
HM77-11003, DCR = 0.233Ω, Note 2
Figure 2. 8V–24V to 5V/1A Buck Converter
Through Hole
L1
150µH
MBR160
12V/1A
R2
13.0k
1%
R1
1.50k
1%
C2
330µF
16V
Note 2: Surface-
mount component.
C1 Nichicon
C2 Nichicon
D1 Motorola
L1 Sumida
UPL1J680MPH, ESR = 0.17Ω
UPL1C331MPH, ESR = 0.12Ω
MBR160
RCH110-151K, DCR = 0.23Ω
Figure 3. 16V–24V to 12V/1A Buck Converter, Through Hole
4-110
April 1998•