English
Language : 

LTC4227_15 Datasheet, PDF (12/22 Pages) Linear Technology – Dual Ideal Diode and Single Hot Swap Controller
LTC4227
Applications Information
Board Presence Detect with EN
If ON is high when the EN pin goes low, indicating a board
presence, the LTC4227 initiates a debounce timing cycle
for contact debounce. Upon board insertion, any bounces
on the EN pin restart the timing cycle. When the debounce
timing cycle is done, the internal fault latches are cleared.
If the EN pin remains low at the end of the timing cycle,
HGATE is charged up with a 10µA current source to turn
on the Hot Swap MOSFET.
If the EN pin goes high, indicating a board removal, the
HGATE pin is pulled low with a 300µA current sink after
a 20µs delay, turning off the Hot Swap MOSFET, without
clearing any latched faults.
Overcurrent Fault
The LTC4227 features an adjustable current limit with
circuit breaker function that protects the external MOSFETs
against short circuits or excessive load current. The voltage
across the external sense resistor, RS, is monitored by an
electronic circuit breaker (ECB) and active current limit
(ACL) amplifier. The electronic circuit breaker will turn off
the Hot Swap MOSFET with a 300µA current from HGATE
to GND if the voltage across the sense resistor exceeds
∆VSENSE(CB) (50mV) for longer than the fault filter delay
configured at the TMR pin.
Active current limiting begins when the sense voltage
exceeds the ACL threshold ∆VSENSE(ACL) (65mV), which
is 1.3× the ECB threshold ∆VSENSE(CB). The gate of the
Hot Swap MOSFET is brought under control by the ACL
amplifier and the output current is regulated to maintain
the ACL threshold across the sense resistor. At this point,
the fault filter starts the timeout with a 100µA current
charging the TMR pin capacitor. If the TMR pin voltage
exceeds its threshold (1.235V), the external MOSFET
turns off with HGATE pulled to ground by 300µA, and its
associated FAULT pulls low.
After the Hot Swap MOSFET turns off, the TMR pin ca-
pacitor is discharged with a 2µA pull-down current until
its threshold reaches 0.2V. This is followed by a cool-off
period of 14 timing cycles at the TMR pin. For the latch-
off part (LTC4227-1/LTC4227-3), the HGATE pin voltage
does not restart at the end of the cool-off period, unless
the latched fault is cleared by pulling the ON pin low or
toggling the EN pin from high to low. For the auto-retry
part (LTC4227-2/LTC4227-4), the latched fault is cleared
automatically at the end of the cool-off period, and the
HGATE pin restarts charging up to turn on the MOSFET.
Figure 4 shows an overcurrent fault on the 12V output.
In the event of a severe short-circuit fault on the 12V
output as shown in Figure 5, the output current can surge
to tens of amperes. The LTC4227 responds within 1µs to
bring the current under control by pulling the HGATE to
OUT voltage down to zero volts. Almost immediately, the
gate of the Hot Swap MOSFET recovers due to the RHG
and CHG network, and current is actively limited until the
electronic circuit breaker times out. Due to parasitic sup-
ply lead inductance, an input supply without any bypass
capacitor may collapse during the high current surge and
then spike upwards when the current is interrupted. Figure 9
shows the input supply transient suppressors consisting
of Z1, RSNUB1, CSNUB1 and Z2, RSNUB2, CSNUB2 for the two
supplies if there is no input capacitance.
OUT
10V/DIV
HGATE
10V/DIV
ILOAD
20A/DIV
200µs/DIV
4227 F04
Figure 4. Overcurrent Fault on 12V Output
OUT
10V/DIV
HGATE
10V/DIV
ILOAD
20A/DIV
2µs/DIV
4227 F05
Figure 5. Severe Short-Circuit on 12V Output
12
For more information www.linear.com/LTC4227
422712fa