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FAN6862L Datasheet, PDF (10/16 Pages) Fairchild Semiconductor – Highly Integrated Green-Mode PWM Controller
Operation Description
Startup Operation
Figure 21 shows a typical startup circuit and
transformer auxiliary winding for a typical application.
Before FAN6862R/L begins switching operation, it
consumes only startup current (typically 8μA) and the
current supplied through the startup resistor charges
the VDD capacitor (CDD). When VDD reaches the turn-on
voltage of 16V (VDD-ON), FAN6862R/L begins switching
and the current consumed increases to 3mA. Then the
power required is supplied from the transformer
auxiliary winding. The large hysteresis of VDD (8.5V)
provides more holdup time, which allows using a small
capacitor for VDD. The startup resistor is typically
connected to AC line for a fast reset of latch protection.
Frequency
+4.2kHz
65kHz
-4.2kHz
+2.9kHz
22.5kHz
-2.9kHz
PWM
Frequency
VFB-ZDC VFB -G
VFB -N
VFB
Figure 22. PWM Frequency
Vo
VFB
VFB.ZDC
(1.7V)
Ids
Figure 21. Startup Circuit
Switching
Disabled
Switching
Disabled
Figure 23. Burst-Mode Operation
Green-Mode Operation
The FAN6862R/L uses feedback voltage (VFB) as an
indicator of the output load and modulates the PWM
frequency, as shown in Figure 22, such that the
switching frequency decreases as load decreases. In
heavy-load conditions, the switching frequency is
65KHz. Once VFB decreases below VFB-N (2.5V), the
PWM frequency starts to linearly decrease from 65KHz
to 22.5kHz to reduce the switching losses. As VFB
decreases below VFB-G (2.1V), the switching frequency
is fixed at 22.5kHz and FAN6862R/L enters “deep”
green mode, where the operating current decreases to
2.5mA (maximum), further reducing the standby power
consumption. As VFB decreases below VFB-ZDC (1.7V),
FAN6862R/L enters burst-mode operation. When VFB
drops below VFB-ZDC, switching stops and the output
voltage starts to drop, which causes the feedback
voltage to rise. Once VFB rises above VFB-ZDC, switching
resumes. Burst mode alternately enables and disables
switching, thereby reducing switching loss in standby
mode, as shown in Figure 23.
Frequency Hopping
EMI reduction is accomplished by frequency hopping,
which spreads the energy over a wider frequency range
than the bandwidth measured by the EMI test
equipment. An internal frequency hopping circuit
changes the switching frequency between 60.8kHz and
69.2kHz with a period of 4.4ms, as shown in Figure 24.
Figure 24. Frequency Hopping
© 2009 Fairchild Semiconductor Corporation
FAN6862R/L • Rev. 1.0.0
10
www.fairchildsemi.com